实验流体力学2011,Vol.25Issue(2):17-21,5.
进气系统对无阀脉冲爆震发动机性能影响试验研究
Experimental study for the effect of induction systems on valveless pulse detonation engine
摘要
Abstract
This paper addressed the operation and propulsive performance of air-breathing pulse detonation engine with inner diameters of 50mm based on the semi-free-jet simulated ground experiments. Gasoline was used as the liquid fuel and the air was supplied upstream of the air inlet by a semi subsonic free flow field. Six assembled induction systems were employed to investigate the effects of some geometry parameters, such as inlet area, blockage ratio of circumferential seam, length of conical inner body, on PDE performance. The results indicated no matter which induction system was used, PDE can be initiated by one-step with low-energy ignition system (less than 50mJ). The average thrust of PDE with six all assembled inlet systems increased as the operation frequency increased, while the increasing ratio of average thrust was faster when the area of coming air injector and inlet were both less. As the blockage ratio of circumferential seam increased, the PDE average thrust decrease slightly.关键词
脉冲爆震发动机/进气道/进气系统/平均推力Key words
pulse detonation engine/ inlet/ induction system/ average thrust分类
航空航天引用本文复制引用
王治武,严传俊,郑龙席,范玮..进气系统对无阀脉冲爆震发动机性能影响试验研究[J].实验流体力学,2011,25(2):17-21,5.基金项目
国家自然科学基金资助项目(50336030) (50336030)
陕西省自然科学基金资助项目(S2010JC3660) (S2010JC3660)
西北工业大学科技创新基金资助项目(2008KJ02021) (2008KJ02021)