石油与天然气化工2009,Vol.38Issue(5):453-455,3.DOI:10.3969/j.issn.1007-3426.2009.05.023
钻井液用铁离子络合物型除硫剂的室内评价
Laboratory-Test of Drilling Fluids with Ferric Ion Complex Type Sulphide Scavenger
马其金 1杨眉 1张启根 1苏银华 1谢显涛2
作者信息
- 1. 四川华油集团有限责任公司油化分公司
- 2. 川庆钻探工程公司川西钻探公司
- 折叠
摘要
Abstract
The performance of the ferric ion complex sulphide scavenger is tested in laboratory. This sulphide scavenger is synthesized by ferrous and derivate of carbohydrates. It is easy dissolved in water-base drilling fluid and cannot subside when the pH value is 12, while the desulphuration efficiency can get as high as 98.6% as the pH value of drilling fluids is 9. Under 70℃, the highest corrosion control efficiency value is 71.23 %, which can remarkably slow down the corrosion rate for drilling rig. The sulphide scavenger is good compatible with poly-sulfonate drilling fluids, and won't obviously affect the rheology and filtration loss of the drilling fluid. The desulfuration has rapid reaction velocity and high reaction effectiveness. It not only prolong the life of drilling rig, but also protect people not be infected by H_2S.关键词
钻井液/硫化氢/除硫剂/缓蚀剂/钻井液流变性Key words
drilling fluid/hydrogen sulphide/sulphide scavenger/corrosion inhibitor/drilling fluid rheological property分类
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马其金,杨眉,张启根,苏银华,谢显涛..钻井液用铁离子络合物型除硫剂的室内评价[J].石油与天然气化工,2009,38(5):453-455,3.