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电测深法岩溶路基注浆质量检测模型试验研究

任新红 谢强 郑立宁 肖学仁 郭永春

水文地质工程地质2011,Vol.38Issue(5):49-53,57,6.
水文地质工程地质2011,Vol.38Issue(5):49-53,57,6.

电测深法岩溶路基注浆质量检测模型试验研究

A study of the quality test model of resistivity sounding for detecting grouting effect of karst roadbed

任新红 1谢强 1郑立宁 1肖学仁 1郭永春1

作者信息

  • 1. 西南交通大学土木工程学院,成都610031
  • 折叠

摘要

Abstract

Due to the difficulty of quality test of karst roadbed, based on typical field geological sections, a model of stenopeic limestone is established, and analysis of the results of resistivity sounding test on many sections before and after grouting is carried out, and comparison with the real diffusion area in the model is also performed. The results suggest that after the cement flow is injected into the model, the apparent resistivity decrease more obviously than before grouting. When the decreased extent is equal to or above 15% after grouting, the grouting effect is good and the rational test time is 7 days after grouting. The field tests basically verify the results of the model tests. However, the field tests are significantly controlled by ground water level. As a result, the partial faults of the judgment may be caused.

关键词

电测深法/模型试验/岩溶路基/注浆质量/检测

Key words

resistivity sounding/ model test/ karst roadbed/ grouting quality/ detection

分类

天文与地球科学

引用本文复制引用

任新红,谢强,郑立宁,肖学仁,郭永春..电测深法岩溶路基注浆质量检测模型试验研究[J].水文地质工程地质,2011,38(5):49-53,57,6.

基金项目

铁道部科技研究开发计划项目(2009G010-A) (2009G010-A)

中央高校基本科研业务费专项资金资助(2010XS08) (2010XS08)

水文地质工程地质

OA北大核心CSCDCSTPCD

1000-3665

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