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钢管再生混凝土短柱偏压性能实验

张卫东 王振波 丁海军

大庆石油学院学报2011,Vol.35Issue(5):88-91,96,5.
大庆石油学院学报2011,Vol.35Issue(5):88-91,96,5.

钢管再生混凝土短柱偏压性能实验

张卫东 1王振波 2丁海军2

作者信息

  • 1. 宿迁学院建筑工程系,江苏宿迁223800
  • 2. 南京工业大学土木工程学院,江苏南京210009
  • 折叠

摘要

Abstract

Based on eccentric compressive tests of 15 different replacement percentage of recycled concrete filled steel tubes short columns, macroscopic characters of deformation, force-longitudinal strain curves, failure modes and failure mechanism are studied in this paper. The test results showed that the replacement percentage of recycled concrete is an important parameter to the mechanical properties of the recycled concrete filled steel tubes short columns. In the same condition, when the replacement percentage of recycled concrete increases, the bearing capacity will decline to 20%; shrinkage ratio will increase and reduce support to steel tubes, local buckling is accelerated and the bearing capacity will decline.

关键词

钢管再生混凝土/偏压实验/取代率/收缩率

Key words

recycled concrete filled steel tube/eccentric compression test/replacement percentage/shrinkage ratio

分类

建筑与水利

引用本文复制引用

张卫东,王振波,丁海军..钢管再生混凝土短柱偏压性能实验[J].大庆石油学院学报,2011,35(5):88-91,96,5.

基金项目

住建部科学技术项目(2008-k1-11) (2008-k1-11)

江苏省教育厅自然科学项目(11KJD560003) (11KJD560003)

宿迁市科技局项目(B2010021) (B2010021)

江苏省高校"青蓝工程"对象项目(苏教师[2010]16号) (苏教师[2010]16号)

大庆石油学院学报

OA北大核心CSTPCD

2095-4107

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