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斜井二次涌水原因分析及注浆治理措施

钱自卫 马保明 姜振泉 刘鹏

水文地质工程地质2012,Vol.39Issue(2):19-22,4.
水文地质工程地质2012,Vol.39Issue(2):19-22,4.

斜井二次涌水原因分析及注浆治理措施

Hydrogeological analysis and control of groundwater inrush for the second time in an inclined shaft

钱自卫 1马保明 2姜振泉 1刘鹏2

作者信息

  • 1. 中国矿业大学资源与地球科学学院,徐州 221116
  • 2. 山西潞安集团黑龙煤业有限公司,临汾 401201
  • 折叠

摘要

Abstract

A groundwater inrush occurred again when excavation came to the pregrouting interval in the auxiliary inclined shaft, which submersed the shaft of the Heilong Coal Mine in Shanxi. The main cause was that the poorness of the fracture stability was formed during the interaction of soft clay and grout in the first grouting process. The method "distributary to relieve pressure then to prevent water inflow" was taken, thus the uncontrollable gushing was changed into controllable gushing and grouting. The borehole was used to examine the effect of the grouting, and the results show that the effect was good. This paper provides references for similar grouting in rock mass which is filled with soft clay.

关键词

涌水/软粘土充填/充填体稳定性/注浆治理

Key words

water inflow/soft clay filling/ filling body stability/ grouting control

分类

天文与地球科学

引用本文复制引用

钱自卫,马保明,姜振泉,刘鹏..斜井二次涌水原因分析及注浆治理措施[J].水文地质工程地质,2012,39(2):19-22,4.

基金项目

中国矿业大学青年科研基金资助项目(2009A029) (2009A029)

深部岩土力学与地下工程国家重点实验室博士后专项基金(PD1012) (PD1012)

水文地质工程地质

OA北大核心CSCDCSTPCD

1000-3665

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