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动静力排水固结法处理淤泥地基的现场试验研究

张丽娟 李彰明

路基工程Issue(2):81-85,5.
路基工程Issue(2):81-85,5.

动静力排水固结法处理淤泥地基的现场试验研究

On-site Experimental Study on Disposal of Muck Foundation by Dynamic-static Drainage Consolidation Method

张丽娟 1李彰明1

作者信息

  • 1. 广东工业大学土木与交通工程学院,广州510006
  • 折叠

摘要

Abstract

Combining with the project of muck foundation disposal at Nansha Port, Guangzhou and using the indexes, such as excess pore water pressure, layered settlement and shearing strength, the depth and the effect of the reinforcement on muck foundation by means of dynamic-static drainage consolidation are studied through on-site experiment. The result shows that the increment of total tamping energy can increase the effective reinforced depth obviously. When tamping energy is given, tamping four or five times with the tamping energy in single point every time to be controlled less than 900 kN. m has superior reinforced effect and depth than tamping three times ; the reinforced depth and effect by means of heavy hammer and low drop distance tamping are superior to those by light hammer and high drop distance.

关键词

动静力排水固结/加固深度/加固效果/淤泥质地基处理

Key words

dynamic-static drainage consolidation/reinforced depth/reinforced effect/muck foundation disposal

分类

建筑与水利

引用本文复制引用

张丽娟,李彰明..动静力排水固结法处理淤泥地基的现场试验研究[J].路基工程,2012,(2):81-85,5.

基金项目

广东省自然科学基金项目 ()

路基工程

1003-8825

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