理化检验:物理分册2012,Vol.48Issue(8):528-531,4.
某井P110EU油管应力腐蚀断裂失效分析
Failure Analysis on Stress Corrosion Fracture of P110EU Tubing in a Well
韩燕 1赵密峰 2林冠发 1赵雪会 1蔡锐1
作者信息
- 1. 中国石油集团石油管工程技术研究院,西安710065
- 2. 塔里木油田,库尔勒841000
- 折叠
摘要
Abstract
Through physical and chemical properties testing, SEM and EDS analysis, the fractured P110EU tubing in a well was analyzed. The results show that the fracture property of the tubing was sulfide stress corrosion fracture, which was caused by mechanical damage on outer wall of the tubing. High hardness and the presence of sulfate-reducing bacteria were the main reason leading to the tubing fracture eventually.关键词
P110EU油管/硫化物应力腐蚀断裂/硫酸盐还原菌Key words
P110EU tubing/sulfide stress corrosion fracture/sulfate-reducing bacteria分类
石油、天然气工程引用本文复制引用
韩燕,赵密峰,林冠发,赵雪会,蔡锐..某井P110EU油管应力腐蚀断裂失效分析[J].理化检验:物理分册,2012,48(8):528-531,4.