航空材料学报2013,Vol.33Issue(1):86-92,7.DOI:10.3969/j.issn.1005-5053.2013.1.015
基于k样本Anderson-Darling检验的混杂铺层层合板挖补修理后拉伸性能研究
Experimental Investigation of Tensile Behavior of Hybrid Laminates Repaired by Scarfing Method Based on k-sample Anderson-Darling Test
刘遂 1关志东 1郭霞 1薛斌 1席国芬 2蔡婧2
作者信息
- 1. 航空航天大学航空科学与工程学院,北京100191
- 2. 中国商飞设计研发中心,上海200232
- 折叠
摘要
Abstract
Experimental study on tensile behavior of hybrid plain woven fabric laminate repaired by scarfing method was conducted in the paper. In order to analyze experimental results, k-sample Anderson-Darling test was adopted in the study to investigate the influence of scarf ratio, repair methods and initial damage diameters to the tensile behaviors of repaired specimens. Experimental results indicate scarfing repair can recover the tensile strength of laminate well. After thorough comparison, the study demonstrates that the tensile strength of full depth scarfing specimen can achieve the level of intact panel when scarf ratio exceeds 1 ;20 and for half depth scarfing specimen, the threshold of scarf ratio is 1:10. Test results also reveal when the scarf ratio is fixed, changing the diameter of initial damage could hardly affect the tensile strength and failure mode of scarfing repaired specimens. Conclusions of the investigation provide insight into scarfing repair design method on hybrid plain woven fabric laminate.关键词
挖补修理/混杂铺层/拉伸强度/破坏模式/k样本Anderson-Darling检验Key words
scarfing repair/ hybrid laminate/ tensile strength/ failure mode/ k-sample Anderson-Darling test分类
航空航天引用本文复制引用
刘遂,关志东,郭霞,薛斌,席国芬,蔡婧..基于k样本Anderson-Darling检验的混杂铺层层合板挖补修理后拉伸性能研究[J].航空材料学报,2013,33(1):86-92,7.