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300MW锅炉再热汽温低的原因分析及改造

赵振宁 王晶晶 徐立伟 姚万业 童家麟

中国电力2012,Vol.45Issue(12):21-25,5.
中国电力2012,Vol.45Issue(12):21-25,5.

300MW锅炉再热汽温低的原因分析及改造

Cause Analysis for Low Reheat Steam Temperature and Transformations of 300-MW Boilers

赵振宁 1王晶晶 1徐立伟 2姚万业 3童家麟2

作者信息

  • 1. 华北电力科学研究院有限责任公司,北京 100045
  • 2. 华北电力大学,河北保定071003
  • 3. 华北电力大学,北京 102206
  • 折叠

摘要

Abstract

For the 300-MW subcritical boiler in a power plant, the steam temperature at the outlet of the reheater has always been lower than the designed value after the turbine through-flow transformation. Through the analysis on the data from the reheat steam temperature adjustment test, it is observed that the steam temperature at the inlet of the reheater is much lower than the designed value. Based on the thermal balance calculation, three schemes for increasing the capacity of the reheater are proposed. After comparison, the most reasonable one is selected and put into practice. The performance test after the transformation indicates that the reheat steam temperature at the outlet of the reheater is improved significantly, reaching the designed value of 541℃ with the economic efficiency of the plant also improved greatly.

关键词

300 MW机组/通流改造/再热汽温/增容改造

Key words

300 MW unit/ through-flow transformation/ reheat steam temperature/ capacity-increasing transformation

分类

能源科技

引用本文复制引用

赵振宁,王晶晶,徐立伟,姚万业,童家麟..300MW锅炉再热汽温低的原因分析及改造[J].中国电力,2012,45(12):21-25,5.

中国电力

OA北大核心CSCDCSTPCD

1004-9649

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