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机器人自动上箱系统在卷烟装封箱机组的应用

杨剑锋 徐智勇 赵云斌 关宏

烟草科技Issue(2):20-23,4.
烟草科技Issue(2):20-23,4.

机器人自动上箱系统在卷烟装封箱机组的应用

Application of Robot for Automatic Case Loading System in Cigarette Case Filling and Sealing Machine

杨剑锋 1徐智勇 1赵云斌 1关宏2

作者信息

  • 1. 红云红河烟草(集团)有限责任公司曲靖卷烟厂,655001
  • 2. 北京达特烟草成套设备技术开发有限责任公司,100176
  • 折叠

摘要

Abstract

For eliminating the shortcomings associated with manual operation such as low efficiency and high error rate and creating a smooth connection with material logistics system in terms of automation and informatization, the case loading in cigarette case filling and sealing system was upgraded with industrial robot and image recognition technologies. The system adopted 6-anticulate light-duty industrial robot in order to grasp the case more flexibly and used large area cellular vacuum chuck with multi-stage vacuum generator as clamps to improve system reliability. An image recognition system collected the information and data about the cases via an industrial intelligent camera and carried out image data processing. The practical application showed that the robot system realized automatic tape unloosing, recognizing, feeding and grabbing, and the seamless connection between feeding station and AGV (Automatic Guided Vehicle) system. Comparing with traditional case handling, the proportion of compound cycle of AGVs increased by 40%, it allowed to reduce the number of AGVs accordingly. Comparing with traditional manual case loading, the accuracy rate of robot case loading was up to 99%. The labor intensity of operators was reduced, and working efficiency was improved.

关键词

装封箱机组/机器人/上箱系统/图像识别/自动导引车系统

Key words

Case filling and sealing machine/Robot/Case loading system/Image recognition/Automatic guided vehicle system

分类

管理科学

引用本文复制引用

杨剑锋,徐智勇,赵云斌,关宏..机器人自动上箱系统在卷烟装封箱机组的应用[J].烟草科技,2013,(2):20-23,4.

烟草科技

OA北大核心CSTPCD

1002-0861

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