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粉末火箭发动机推力调节试验研究

张胜敏 杨玉新 胡春波

固体火箭技术Issue(3):347-350,4.
固体火箭技术Issue(3):347-350,4.DOI:10.7673/j.issn.1006-2793.2015.03.009

粉末火箭发动机推力调节试验研究

Experimental investigation on thrust regulation of powdered rocket motor

张胜敏 1杨玉新 1胡春波2

作者信息

  • 1. 中国航天科技集团公司四院四十一所,西安 710025
  • 2. 西北工业大学,西安 710072
  • 折叠

摘要

Abstract

An experiment system of powdered rocket motor was established to investigate some key technologies, such as multi⁃ple start⁃ups and thrust regulation and so on, large numbers of experiments were conducted. The results indicat that under the effect of high energy spark plug,powered rocket motor can realize multiple start⁃ups and shutdown.Moreover startup and shutdown times, the time intervals can be regulated randomly. By adjusting the flow rate of the powder fuel and oxidant, powered rocket motor can a⁃chieve thrust control technology,and thrust regulation ratio reaches 6.5.

关键词

粉末火箭发动机/试验研究/推力调节/点火/关机

Key words

powdered rocket motor/experimental investigation/thrust regulation/ignition/shutoff

分类

航空航天

引用本文复制引用

张胜敏,杨玉新,胡春波..粉末火箭发动机推力调节试验研究[J].固体火箭技术,2015,(3):347-350,4.

固体火箭技术

OA北大核心CSCDCSTPCD

1006-2793

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