石油与天然气化工Issue(1):21-24,4.DOI:10.3969/j.issn.1007-3426.2015.01.005
塔二联轻烃站脱硫系统参数调整分析
Parameters adjustment analysis of desulfurization system of Tahe 2# light hydrocarbon station
马国光 1曹连进 1钟荣强 2季夏夏1
作者信息
- 1. 油气藏地质及开发工程”国家重点实验室·西南石油大学
- 2. 中国石化西北油田分公司
- 折叠
摘要
Abstract
Aiming at the fluctuation of H 2 S content in natural gas and the unqualified natural gas , the sensitivity analysis of operating parameters that affect the desulfurization device were made .The analysis result indicates that operating pressure ,temperature of the absorber and MDEA circulation flow rate have little effect on H2 S content in sweet gas ,but operating parameters of regenerator have a great influence on desulfurization effect .Therefore ,only operating parameters of MDEA regenera‐tor were adjusted .The results show that when the mass fraction of H2S in natural gas increased by 58% ,it can effectively reduce the content of H2 S in the sweet gas to reach the standard by slightly ad‐justing operating pressure and temperature of MDEA regenerator .关键词
脱硫装置/敏感性/参数调整/H2S含量Key words
desulfurization device/sensitivity/parameter adjustment/H2 S content分类
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马国光,曹连进,钟荣强,季夏夏..塔二联轻烃站脱硫系统参数调整分析[J].石油与天然气化工,2015,(1):21-24,4.