石油钻采工艺Issue(4):54-56,3.DOI:10.13639/j.odpt.2014.04.014
低含量 KCl 钻井液在苏里格气田的应用
Application of low content KCl drilling fluid in Sulige Gas Field
蒋明 1罗树祥 1王先洲 1邓增库 1张刚 2管风营1
作者信息
- 1. 渤海钻探第五钻井工程分公司,河北河间 062450
- 2. 渤海钻探泥浆技术服务分公司,天津 300280
- 折叠
摘要
Abstract
Severe borehole collapse occur easily in mudstone formations of Shiqianfeng Formation and Shihezi Formation of Sulige Gas Field, and troubles like hole collapse reaming, sticking, filling the hole and sidetracking often occur also. In view of the formation rock properties and characteristics of Sulige Gas Field, study was conducted on low content KCl drilling fluid; the inhibition and anti-collapse performance of the drilling fluid system is improved by maintaining 0.8%-1.0% of KCl in polysulfonate drilling fluid. Its appli-cation in two wells shows that this system has generated strong inhibition and clear sand specimen with no collapse and no obstructions in wiper trips; it has favorable performance in plugging and side-wall building and rheological property; the filter cake is smooth and tight and has stable performance; there is no discharge of drilling fluid; all of these properties satisfactorily meet the downhole service requirements and provide experiences for safe and efficient development of Sulige Gas Field.关键词
低含量 KCl/井壁稳定/水化膨胀/流变性/苏里格气田Key words
low content KCl/borehole stability/hydration swelling/rheology/Sulige Gas Field分类
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蒋明,罗树祥,王先洲,邓增库,张刚,管风营..低含量 KCl 钻井液在苏里格气田的应用[J].石油钻采工艺,2014,(4):54-56,3.