| 注册
首页|期刊导航|水资源与水工程学报|导流隧洞出口消力池体型优化数值模拟与试验研究

导流隧洞出口消力池体型优化数值模拟与试验研究

张铭 杨敏 刘金星

水资源与水工程学报Issue(1):166-170,5.
水资源与水工程学报Issue(1):166-170,5.DOI:10.11705/j.issn.1672-643X.2015.01.032

导流隧洞出口消力池体型优化数值模拟与试验研究

Experiment and numerical simulation of stilling pool shape optimization at diversion tunnel outlet

张铭 1杨敏 1刘金星1

作者信息

  • 1. 天津大学水利工程仿真与安全国家重点实验室,天津300072
  • 折叠

摘要

Abstract

Through numerical simulation and model test on diversion tunnel discharge of water conservan-cy project in Aertash of Xinjiang,the paper optimized the shape of stilling pool, and compared water level line, energy dissipation, the maximum underflow speed and the flow pattern of tailwater canal of the opti-mization scheme with that of original design scheme.The results show that after the optimization, the maximum water depth decreased 2.05 m in the stilling basin, the energy dissipation ratio increased by 12%, the maximum underflow velocity reduced by 28%, and the velocity in tailwater canal decreased by 66 .7%.The hydraulic characteristics indicators show that the stilling pool after optimization performs a better characteristics compared with that of the original design scheme.

关键词

导流/消力池/水面线/消能率/尾渠流速

Key words

diversion/stilling pool/water level line/energy dissipation rate/velocity of tailwater canal

分类

建筑与水利

引用本文复制引用

张铭,杨敏,刘金星..导流隧洞出口消力池体型优化数值模拟与试验研究[J].水资源与水工程学报,2015,(1):166-170,5.

水资源与水工程学报

OACSTPCD

1672-643X

访问量0
|
下载量0
段落导航相关论文