石油与天然气化工Issue(4):8-13,6.DOI:10.3969/j.issn.1007-3426.2015.04.002
炼油厂硫磺回收联合装置SO2达标排放对策
Countermeasures of SO2 up-to-standard emission of the sulfur recovery unit in a refinery
刘勇 1张万全 1李峰 1袁侃 1姚孙坤2
作者信息
- 1. 中国石油四川石化有限责任公司
- 2. 四川天一科技有限公司
- 折叠
摘要
Abstract
A technical investigation ,including process and system design ,equipments and facili‐ties ,and operations etc .,was carried out in a refinery to find the reasons of SO 2 emission in the tail gas beyond the standard .The results showed that the direct reason was oil and light hydrocarbon car‐rying with rich amine solution .Further ,investigation and analysis indicated that a series of reasons resulted in the oil and light hydrocarbon carrying with rich amine solution .The reasons included small size of gas‐liquid separator ,lower temperature of lean amine solution ,higher temperature of recycle hydrocarbon gas in up‐stream units ,faulting design of oil skimming in amine flash drum of up‐stream units ,and insufficient design flow rate of the torch gas from rich amine flash drum .To solve the a‐bove problems ,some corresponding solutions were put forward including the design of system and process flow design ,process indexes ,operation ,and equipment modification .关键词
排放/SO2/调查/分析/硫磺回收/炼油厂Key words
emission/sulfur dioxide/investigation/analysis/sulfur recovery/refinery分类
能源科技引用本文复制引用
刘勇,张万全,李峰,袁侃,姚孙坤..炼油厂硫磺回收联合装置SO2达标排放对策[J].石油与天然气化工,2015,(4):8-13,6.