热力发电Issue(8):121-124,4.DOI:10.3969/j.issn.1002-3364.2015.08.121
湿法脱硫吸收塔浆液起泡的影响因素
Influence factors of absorber slurry foaming in wet limestone-gypsum flue gas desulphurization systems
李兴华 1金万元 2张劲松 2贾西部1
作者信息
- 1. 西安热工研究院有限公司,陕西 西安 710032
- 2. 内蒙古岱海发电有限公司,内蒙古 凉城 013750
- 折叠
摘要
Abstract
The absorber slurry foaming problem occurs commonly in wet limestone-gypsum flue gas desul-phurization (FGD)systems,which may result in many adverse effects on the FGD system's performance. Possible causes of this problem were analyzed based on its formation mechanism.In addition,a long-term tracking test on the FGD system of a power plant was conducted,and the influence factors of the absorber slurry foaming problem were found out.Moreover,several countermeasures were proposed.关键词
烟气/湿法脱硫/脱硫装置/吸收塔/浆液起泡Key words
flue gas/wet desulphurization/desulphurization device/absorber/slurry foaming分类
信息技术与安全科学引用本文复制引用
李兴华,金万元,张劲松,贾西部..湿法脱硫吸收塔浆液起泡的影响因素[J].热力发电,2015,(8):121-124,4.