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管道漏水引起黄土滑坡失稳机理研究

刘朋飞 李滨 高扬

南水北调与水利科技Issue(2):49-51,103,4.
南水北调与水利科技Issue(2):49-51,103,4.DOI:10.3724/SP.J.1201.2013.02049

管道漏水引起黄土滑坡失稳机理研究

Study on the Instability Mechanism of Loess Landslide Caused by Pipeline Leakage

刘朋飞 1李滨 2高扬1

作者信息

  • 1. 长安大学地质工程与测绘学院,西安710054
  • 2. 中国地质科学院地质力学研究所,北京 100081
  • 折叠

摘要

Abstract

A major geological disaster of landslide happened in Dongxiang County of Gansu Province on March 2nd ,2011 ,which threatened the safety of two thirds of the total population .The landslide survey was performed to analyze the development char‐acteristics of landslide .The moisture absorption of soil‐water characteristic curve test was conducted on the unsaturated loess , and the seepage field of landslide caused by the pipeline leakage was simulated based on the saturated and unsaturated theory . The variation of seepage field of loess landslide caused by the pipeline leakage was analyzed .Finally ,the original slope stability was compared with and the slope stability caused by the pipeline leakage ,which confirmed that the pipeline leakage induces loess landslide .

关键词

黄土/滑坡/非饱和渗流/强度折减

Key words

loess/landslide/unsaturated seepage/strength reduction

分类

地质学

引用本文复制引用

刘朋飞,李滨,高扬..管道漏水引起黄土滑坡失稳机理研究[J].南水北调与水利科技,2013,(2):49-51,103,4.

基金项目

国家自然科学基金“多级旋转型黄土滑坡形成机理研究”(4110264) (4110264)

南水北调与水利科技

OA北大核心CSCDCSTPCD

2096-8086

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