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660 MW机组中调门控制指令异常波动原因分析及处理

张兴

浙江电力Issue(2):45-47,3.
浙江电力Issue(2):45-47,3.

660 MW机组中调门控制指令异常波动原因分析及处理

Cause Analysis and Treatment on Control Instruction Fluctuation of Medium-pressure Regulating Valve

张兴1

作者信息

  • 1. 中国大唐集团科学技术研究院有限公司华东分公司,合肥 230088
  • 折叠

摘要

Abstract

Single valve and sequence valve can not be normally switched due to control instruction fluctuation of medium-pressure regulating valve of steam turbine after integration of 660 MW units. The paper analyzes control mechanism of medium-pressure regulating valve of steam turbine DEH (digital electro-hydraulic control system) and expounds problems of major parameter control during generating units startup by comparing the examples. The method of eliminating control instruction fluctuation of medium-pressure regulating valve through control modes switching can be reference for steam turbine turning and controlling in other power plants.

关键词

DEH/中调门/阀位指令/旁路模式

Key words

DEH/medium-pressure regulating valve/valve position instruction/bypass mode

分类

能源科技

引用本文复制引用

张兴..660 MW机组中调门控制指令异常波动原因分析及处理[J].浙江电力,2016,(2):45-47,3.

浙江电力

1007-1881

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