中国电力2017,Vol.50Issue(5):33-38,6.DOI:10.11930/j.issn.1004-9649.2017.05.033.06
一起因特高压直流事故引起的AGC指令异常分析及整改措施
Analysis and Treatment of Abnormal AGC Orders Caused by a UHVDC Block Fault
孙文多 1卢敏 1项中明 1倪秋龙 1刘俊伟 2高强 1金啸虎1
作者信息
- 1. 国网浙江省电力公司,浙江杭州310007
- 2. 国电南瑞科技股份有限公司,江苏南京210003
- 折叠
摘要
Abstract
Based on analysis of AGC orders and feedback data during an UHVDC block fault accident treatment,abnormal conditions in automatic generation control system are discussed and rectification measures are proposed.Automatic generation control (AGC) strategies in Zhejiang power grid and accident treatment of one ±800 kV Yibin-Jinhua DC unipolar block fault performed by provincial dispatcher are introduced.System defects are found after reviewing data changes.Improvement measures in transmission mechanism of power importing data,control of low frequency and dynamic dead band optimization are proposed.These measures are already operated in actual power grid system operation which have instructive significance for UHVDC export/import power grid.关键词
特高压直流/自动发电控制/事故处置/区域网调节功率/ARR动态死区Key words
UHVDC/automatic generation control (AGC)/accident disposal/area regulation requirement/dynamic dead band of ARR分类
信息技术与安全科学引用本文复制引用
孙文多,卢敏,项中明,倪秋龙,刘俊伟,高强,金啸虎..一起因特高压直流事故引起的AGC指令异常分析及整改措施[J].中国电力,2017,50(5):33-38,6.