| 注册
首页|期刊导航|中国电力|IGCC燃机入口合成气温度低导致跳机问题分析及解决措施

IGCC燃机入口合成气温度低导致跳机问题分析及解决措施

丁建博 赵雁鹏 王健

中国电力2018,Vol.51Issue(3):1-6,6.
中国电力2018,Vol.51Issue(3):1-6,6.DOI:10.11930/j.issn.1004-9649.20160466

IGCC燃机入口合成气温度低导致跳机问题分析及解决措施

Analysis on IGCC Unit Trip Caused by Low Temperature at Gas Turbine Inlet and Its Solutions

丁建博 1赵雁鹏 1王健1

作者信息

  • 1. 华能(天津)煤气化发电有限公司,天津 300452
  • 折叠

摘要

Abstract

The gas turbine in Tianjin IGCC demonstration power plant is fueled with light diesel oil and the synthesis gas with low calorific value.After desulfurization,the synthesis gas produced in the gasifier enters the gas turbine through the gas hybrid humidification system.In the synthesis gas exchange process,problems such as the temperature fluctuation in the entrance,the instability of combustion condition occur frequently,resulting in the chain tripping under some severe circumstances.The entrance temperature is a major factor that affects the stable operation of the gas turbine.In this article,the factors that influence the entrance temperature change are analyzed.It is concluded that water accumulated inside the turbine is the main cause of the entrance temperature decrease and direct tripping.Based on the analysis,the technological conditions,the pipeline drainage equipments and the system control logic are improved to prevent such problems from occurring again.

关键词

IGCC/燃气轮机入口温度/合成气/燃气轮机/合成气饱和器

Key words

IGCC/gas turbine inlet temperature/syngas/gas turbine/syngas saturator

分类

信息技术与安全科学

引用本文复制引用

丁建博,赵雁鹏,王健..IGCC燃机入口合成气温度低导致跳机问题分析及解决措施[J].中国电力,2018,51(3):1-6,6.

基金项目

国家科技支撑计划项目(2014BAA05B02).This work is supported by National Science and Technology Support Program (No.2014BAA05B02). (2014BAA05B02)

中国电力

OA北大核心CSCDCSTPCD

1004-9649

访问量0
|
下载量0
段落导航相关论文