红水河2023,Vol.42Issue(6):102-106,122,6.DOI:10.3969/j.issn.1001-408X.2023.06.020
某建成水电站水库渗漏问题分析和研究
Analysis and Research on Reservoir Leakage Problem of a Built Hydropower Station
肖力君 1李正顺 1宋传星1
作者信息
- 1. 中国能源建设集团广西电力设计研究院有限公司, 广西 南宁 530007
- 折叠
摘要
Abstract
A hydropower station is affected by geological conditions and poor curtain grouting effect,and the leakage of the reservoir is generally large after completion.In order to solve the reservoir leakage problem of the hydropower station,the authors expound the investigation and comprehensive analysis of the reservoir leakage through the long-term observation of the groundwater level,hydrogeological test and tracer test,finds out the main leakage areas and leakage channels,and puts forward the leakage treatment scheme.The results show that the leakage of the reservoir is reduced by 1.3 m3/s after reinforcement grouting,which meets the needs of relevant specifications and safe operation of the power station.The engineering experience is summarized:the leakage treatment of mudstone and sandstone interbedded strata with steep dip fissure development needs to focus on controlling the parameters such as grouting hole spacing and grouting pressure.关键词
水库渗漏/泥岩与砂岩互层/地下水位/压水试验/示踪试验/帷幕灌浆Key words
reservoir leakage/mudstone and sandstone interbedded strata/groundwater level/water pressure test/tracer test/curtain grouting分类
建筑与水利引用本文复制引用
肖力君,李正顺,宋传星..某建成水电站水库渗漏问题分析和研究[J].红水河,2023,42(6):102-106,122,6.