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低速大迎角进气道流场测试风洞试验研究

郭佳男

科技创新与应用2024,Vol.14Issue(3):65-68,4.
科技创新与应用2024,Vol.14Issue(3):65-68,4.DOI:10.19981/j.CN23-1581/G3.2024.03.016

低速大迎角进气道流场测试风洞试验研究

郭佳男1

作者信息

  • 1. 中国飞行试验研究院,西安 710089
  • 折叠

摘要

Abstract

In order to meet the inlet test requirements of a certain type of low-speed and high-angle-of-attack flight test,a compound inlet flow field measurement rake was developed,which integrates steady total pressure,dynamic total pressure and steady static pressure,in order to analyze and evaluate the accuracy of parameters measurement of different measurementrake probes,a full-scale wind tunnel test of measurementrake probes was carried out,and the test data were analyzed,the angle characteristic and velocity characteristic of different rake probe were studied,which provides support for the selection of rake probe for subsequent measurement.

关键词

飞行试验/进气道测量耙/探针/风洞试验/总压损失

Key words

flight test/inlet measurement rake/probe/wind tunnel test/total pressure loss

分类

航空航天

引用本文复制引用

郭佳男..低速大迎角进气道流场测试风洞试验研究[J].科技创新与应用,2024,14(3):65-68,4.

科技创新与应用

2095-2945

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