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陈岗新站减压井防渗处理效果分析

陈志昊

江淮水利科技Issue(2):46-49,4.
江淮水利科技Issue(2):46-49,4.DOI:10.20011/j.cnki.JHWR.202402010

陈岗新站减压井防渗处理效果分析

Analysis of the effectiveness of anti-seepage treatment for the Chengang new station pressure relief well

陈志昊1

作者信息

  • 1. 安徽省水利水电勘测设计研究总院股份有限公司,安徽 合肥 230088
  • 折叠

摘要

Abstract

In order to analyze the pressure-reducing performance of relief wells as permanent wells in pumping station forebay,Chengang new station was used as a research object.The seepage stability of the foundation with different relief well arrange-ments was simulated,compared and analyzed,including single-row wells,double-row wells,the combined application of double-row wells and cement-soil replacement.The results showed that the combined application of double-row wells and cement-soil replacement had significant pressure-reducing performance,which was conducive to seepage stability and anti-sliding stability of the foundation,and could provide the design reference for the similar pumping stations.

关键词

泵站/减压井/透水砂基/渗流稳定

Key words

pumping station/relief wel/permeable sand base/operational efficiency analysis

分类

建筑与水利

引用本文复制引用

陈志昊..陈岗新站减压井防渗处理效果分析[J].江淮水利科技,2024,(2):46-49,4.

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