发电技术2024,Vol.45Issue(3):401-411,11.DOI:10.12096/j.2096-4528.pgt.22134
350MW超临界流化床机组深度调峰研究与应用
Research and Application of Deep Peak Shaving of 350 MW Supercritical Fluidized Bed Unit
摘要
Abstract
[Objectives]In order to master the deep peak shaving capability of supercritical circulating fluidized bed units and scientifically participate in the auxiliary service market,it is necessary to conduct in-depth research on the deep peak shaving performance of existing units.[Methods]From the three dimensions of safety,economy and environmental protection,40%and 30%of rated load continuous trial operation,boiler combustion optimization adjustment,boiler efficiency and steam turbine heat consumption rate performance tests were carried out,respectively.More than 10 optimization measures such as single pump operation of feed water pump,pressure curve optimization,boiler oxygen amount,bed pressure adjustment,etc.,were implemented.[Results]The continuous operation of 30%rated load for 12 consecutive days was realized,40%and 30%rated load depth peak-monasizing the peaks affected coal consumption by about 52%,72 g/(kW·h),respectively.[Conclusions]The 350 MW supercritical circulating fluidized bed unit has good deep peak shaving ability.There is no need to transform 30%rated load conditions,and inject oil to stabilize combustion and maintain high efficiency of the boiler.Monitoring parameters for the steam turbine generator unit body,thermal system and auxiliary equipment are normal.The main flue gas pollutants are ultra-low emission.关键词
循环流化床/深度调峰/运行优化/灵活性改造/安全性/经济性Key words
circulating fluidized bed/deep peak shaving/operation optimization/flexibility retrofit/safety/economy分类
能源科技引用本文复制引用
代华松,浦绍旭,柴国旭,金李,陈为平,解明亮..350MW超临界流化床机组深度调峰研究与应用[J].发电技术,2024,45(3):401-411,11.基金项目
中国华电集团有限公司科技项目(CHDKJ20-02-38).Project Supported by Science and Technology Project of China Huadian Group Co.,Ltd.(CHDKJ20-02-38). (CHDKJ20-02-38)