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机器人立式纸箱自动开箱套箱成型系统设计及应用

邓成江 朱清瑞 杨芳 吴永昆 普元成 夏翔 董龙

中国烟草学报2024,Vol.30Issue(2):20-26,7.
中国烟草学报2024,Vol.30Issue(2):20-26,7.DOI:10.16472/j.chinatobacco.2022.T0090

机器人立式纸箱自动开箱套箱成型系统设计及应用

Design and application of automatic unpacking and shaping system for robot vertical carton

邓成江 1朱清瑞 1杨芳 1吴永昆 1普元成 1夏翔 1董龙1

作者信息

  • 1. 云南昆船烟草设备有限公司,昆明市盘龙区人民中路 6 号 650051
  • 折叠

摘要

Abstract

Aiming at the problems of high labor cost,low efficiency and automation in the process of unpacking and shaping by hand before pre-pressing and packing section of tobacco production line in China,a vertical system of automatic unpacking and shaping collaboration between multi equipment based on robot was designed.The system was mainly composed of a robotic grasping system,a feeding device of inner and outer box,a folding device of inner box cover etc.The characteristics of multi degree of freedom motion control of the robot arm in the task space was used to plan a set of technological process suitable for carton shaping,which met the needs of enterprises for high automatic production line.The corrugated carton package of redried strips were tested,the results showed that the system replaced completely the manual to realize unpacking and shaping automatically.The rated production capacity of the system reached 63 boxes/h,the success rate of carton shaping was over 99%,and the number of operators was reduced from 5 to 1 to manage the daily system maintenance.The automation and efficiency of tobacco production line were improved significantly.

关键词

工业机器人/瓦楞纸箱/立式开箱/套箱成型/抓取系统/堆叠上料

Key words

industrial robot/corrugated carton/vertical unpacking/nesting shape/grasping system/stacking and feeding

引用本文复制引用

邓成江,朱清瑞,杨芳,吴永昆,普元成,夏翔,董龙..机器人立式纸箱自动开箱套箱成型系统设计及应用[J].中国烟草学报,2024,30(2):20-26,7.

基金项目

昆明船舶设备集团有限公司"纸箱自动成型关键技术研究"(KC2021203) (KC2021203)

中国烟草学报

OA北大核心CSTPCD

1004-5708

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